ASN Wikibase Occurrence # 76373
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Date: | Monday 16 August 2010 |
Time: | 14:15 |
Type: | Beechcraft V35 Bonanza |
Owner/operator: | Rosemead Properties Inc. |
Registration: | N67311 |
MSN: | D-10333 |
Total airframe hrs: | 2171 hours |
Engine model: | Continental IO-520 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Near Sacramento International Airport (KSMF), California -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | El Monte, CA (EMT) |
Destination airport: | Davis, CA (EDU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that prior to departing for the cross-country flight he had topped off the fuel in both fuel tanks. He took off with the fuel selector positioned to the left tank, and about 1 hour into the flight he switched to the right fuel tank. The remainder of the flight was uneventful until he started the airplane's descent to land. He stated that he switched the fuel selector back to the left fuel tank in preparation for landing. Shortly after he switched the fuel tank, the engine lost power. He repositioned the fuel selector to the right fuel tank and made an unsuccessful attempt to restart the engine. He initiated a forced landing to an open field, and during the descent the airplane struck power lines. The airplane landed hard in a wings-level attitude, substantially damaging the fuselage in the accident sequence. He reported to the Federal Aviation Administration (FAA) inspector who responded to the accident site that he had observed fuel leaking from the fuel cap after takeoff. During the on-scene examination of the airframe the FAA inspector observed fuel stains along the left wing originating from the fuel cap, which was consistent with fuel venting out of the wing. Recovery personnel recovered a minimal amount of fuel during the recovery process and reported that the fuel tanks had not been breached during the accident sequence. Examination of the engine found no evidence of a mechanical failure or malfunction that would have precluded normal operation.
Probable Cause: A total loss of engine power during descent due to fuel exhaustion as a result of the pilot's failure to ensure that the fuel cap was secured during the preflight inspection.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | WPR10LA408 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB
Location
Revision history:
Date/time | Contributor | Updates |
17-Aug-2010 13:36 |
slowkid |
Added |
21-Dec-2016 19:25 |
ASN Update Bot |
Updated [Time, Damage, Category, Investigating agency] |
26-Nov-2017 18:07 |
ASN Update Bot |
Updated [Total fatalities, Total occupants, Nature, Departure airport, Destination airport, Source, Narrative] |
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