Loss of control Accident Cessna 340A N68718,
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ASN Wikibase Occurrence # 78872
 
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Date:Monday 25 October 2010
Time:07:45
Type:Silhouette image of generic C340 model; specific model in this crash may look slightly different    
Cessna 340A
Owner/operator:Pacific Cataract And Laser Institute
Registration: N68718
MSN: 340A1527
Total airframe hrs:6102 hours
Engine model:Continental TSIO-520 SER
Fatalities:Fatalities: 3 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:9 mi NE of Morton, WA -   United States of America
Phase: En route
Nature:Executive
Departure airport:Chehalis, WA (CLS)
Destination airport:Lewiston, ID (LWS)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
About 14 minutes after departing on the cross-country flight in instrument meteorological conditions, the airplane was observed on radar climbing through 14,800 feet mean sea level (msl). At this time, the pilot radioed to air traffic control (ATC) that he was returning to the departure airport. About 7 seconds later, the pilot transmitted that he had lost an engine and again stated that he was returning to the departure airport. About 50 seconds later, the pilot transmitted, “We’re losing it.” There was no further communication with the pilot. Radar data revealed that at 14,800 feet msl the airplane began a right 360-degree turn at 8 degrees per second, and about 120 degrees into the turn, it began a descent averaging 5,783 feet per minute. The airplane remained in a right turn until radar contact was lost at 10,700 feet msl. The airplane impacted a 30-degree slope of a densely forested mountain about 2,940 feet msl in a near vertical, slightly right-wing-low attitude. A logger working in the area reported hearing a “very loud roaring sound,” like an airplane diving toward his location and that it seemed to be “really under power.” The logger described the weather as being “socked in,” with light rain and not much wind.
Postaccident examination revealed that propeller damage was the result of impact forces, with no indications of fatigue or propeller failure before impact. It was also noted that the left propeller was being operated under conditions of some power at impact, while the right propeller was not operating under conditions of significant power at impact. Based on these findings, it is most likely that the pilot experienced a partial loss of power of the right engine and, after incorrectly initiating a right turn into the failed engine, allowed the rate of turn to increase to the point that the airplane became uncontrollable before impact with terrain. The reason for the partial loss of engine power was not determined because postaccident examination of the airframe and both engines did not reveal any mechanical malfunctions or failures that would have precluded normal operation.
Probable Cause: The pilot’s failure to arrest the excessive rate of turn into the failed engine, which resulted in a loss of control and subsequent impact with terrain. Contributing to the accident was a partial loss of engine power for reasons that could not be determined because postaccident examination did not reveal any mechanical malfunctions or failures that would have precluded normal operation.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: WPR11FA029
Status: Investigation completed
Duration: 2 years and 9 months
Download report: Final report

Sources:

NTSB

Location

Revision history:

Date/timeContributorUpdates
26-Oct-2010 03:10 gerard57 Added
26-Oct-2010 03:12 harro Updated [Registration, Cn, Operator, Destination airport]
27-Oct-2010 02:34 gerard57 Updated [Source, Damage, Narrative]
25-Nov-2010 07:56 rvargast17 Updated [Time, Other fatalities, Location, Source]
21-Dec-2016 19:25 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
26-Nov-2017 18:35 ASN Update Bot Updated [Operator, Other fatalities, Nature, Departure airport, Destination airport, Source, Narrative]

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