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Date: | Saturday 21 June 2008 |
Time: | day |
Type: | Beechcraft 99 |
Owner/operator: | Skydive Factory |
Registration: | N99NN |
MSN: | U-10 |
Year of manufacture: | 1968 |
Engine model: | Pratt & Whitney Canada PT6A-20 |
Fatalities: | Fatalities: 1 / Occupants: 12 |
Aircraft damage: | None |
Category: | Accident |
Location: | near Bowling Green Municipal Airport (H19), MO -
United States of America
|
Phase: | En route |
Nature: | Parachuting |
Departure airport: | Bowling Green Municipal Airport (H19), MO |
Destination airport: | Bowling Green Municipal Airport (H19), MO |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The commercial pilot reported that he was en route to a parachutist jump zone on the first of two planned jumps. Prior to the first jump, before he had slowed the airplane, or illuminated the green jump light, indicating that the parachutists had permission to jump, two of the parachutists prematurely jumped. The first parachutist stated that as soon as he jumped, he realized that the airplane was going faster than normal, and he tucked into a ball, barely missing the horizontal stabilizer. According to the other parachutists still aboard, the second jumper exited, and struck the horizontal stabilizer with his head. He never opened his parachute. All of the other parachutists and the pilot stated that the green jump light was never turned on. Post-accident toxicology testing was consistent with impairment of the fatally injured parachutist by recent marijuana use.
Probable Cause and Findings
The National Transportation Safety Board determines the probable cause(s) of this accident to be:
The parachutist's failure to follow procedures/directives by not waiting to jump until the green jump light was illuminated, resulting in his collision with the airplane's tail. Contributing to the accident was the parachutist's impairment by the use of marijuana prior to performing a parachute jump.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | DFW08LA166 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
http://www.dropzone.com/fatalities/Detailed/345.shtml https://app.ntsb.gov/pdfgenerator/ReportGeneratorFile.ashx?EventID=20080627X00939&AKey=1&RType=HTML&IType=LA
History of this aircraft
Other occurrences involving this aircraft
30 April 2022 |
N699CZ |
Freight Runners Express |
0 |
Milwaukee-General Mitchell Airport (MKE/KMKE), Milwaukee, WI |
|
sub |
Gear collapse |
Location
Revision history:
Date/time | Contributor | Updates |
13-Nov-2010 15:30 |
TB |
Added |
12-Apr-2012 12:00 |
TB |
Updated [Narrative] |
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