This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can submit corrected information.
Accident investigation report completed and information captured
Narrative: The flight departed to the east with four skydivers for a local jump. One witness stated that, immediately following the takeoff, about 200 feet above ground level, a "percussive" pop from the engine was heard. Two witnesses stated that the right wing dropped, and the airplane impacted the ground. The airplane was quickly engulfed in a postimpact fire. A postaccident examination of the engine revealed a piece of engine isolator gasket had become wrapped around the carburetor main fuel jet and both magnetos distribution gear had cracked and were missing teeth. The damaged distribution gear teeth were consistent with damage found after an engine experiences a backfire. It could not be determined which magneto failed first or if they both failed simultaneously. The cause of the backfire could not be determined. Further examination of the engine, airframe, and remaining systems revealed no anomalies that would have precluded normal operation. Probable Cause: A loss of engine power due to the magneto failure for undetermined reasons.