Accident Grumman G-44 Widgeon N700BL,
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ASN Wikibase Occurrence # 9713
 
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Date:Thursday 16 May 2002
Time:17:27
Type:Silhouette image of generic G44 model; specific model in this crash may look slightly different    
Grumman G-44 Widgeon
Owner/operator:private
Registration: N700BL
MSN: 1337
Total airframe hrs:3810 hours
Engine model:Continental IO-470
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:1,6 km from Boise Airport, Boise, ID -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:Boise Airport, ID (BOI/KBOI)
Destination airport:Kemmerer Airport, WY (EMM/KEMM)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that shortly after takeoff, the right engine lost power. The pilot stated that he did not feather or secure the engine but concentrated on trying to maintain the single-engine airspeed while attempting to return to the airport. The aircraft was unable to maintain altitude and collided with trees, power lines, and a single-story residence, coming to rest on the roof. During the post-accident inspection of the right engine, the gascolator filter was found covered with metal flakes. A mass amount of the flakes were accumulated at the top end of the filter and blocking the fuel line. Visually and under magnification, the metal flakes varied in size and shape of which many were corkscrew in appearance. The fuel lines downstream of the filter contained a trace amount of fuel. The right side fuel tank was drained. The sump contained debris to include additional metal flakes, screws, washers and pink colored sealant material. The aircraft had just been signed off for the annual inspection. Several maintenance discrepancy items had been found and fixed prior to and after the sign-off. The pilot also reported that during the cross country flight, the right engine had a tendency to stall out below 1,000 rpm. The aircraft flight manual for the accident aircraft indicated in the Emergency Procedures section that if an engine failure occurs after the airplane is airborne, and single engine climb speed is attained, the inoperative engine should be feathered and secured. The single engine rate of climb chart indicated that for the given conditions at the time of the accident, the aircraft should have been able to maintain a positive rate of climb.
Probable Cause: A blocked fuel line that resulted in fuel starvation to the engine and the pilot's failure to follow emergency procedures. A contamination of metal flakes on the fuel filter, and an inadequate annual inspection were factors.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA02FA083
Status: Investigation completed
Duration:
Download report: Final report

Sources:

NTSB: https://www.ntsb.gov/_layouts/ntsb.aviation/brief.aspx?ev_id=20020529X00757&key=1

Location

Revision history:

Date/timeContributorUpdates
25-Feb-2008 12:00 ASN archive Added
13-Jan-2011 14:46 TB Updated [Date, Time, Aircraft type, Registration, Cn, Operator, Total fatalities, Total occupants, Other fatalities, Location, Country, Phase, Departure airport, Damage, Narrative]
21-Dec-2016 19:13 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:14 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:16 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
21-Dec-2016 19:20 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
09-Dec-2017 16:42 ASN Update Bot Updated [Cn, Operator, Nature, Departure airport, Destination airport, Source, Narrative]
16-Sep-2023 11:53 Ron Averes Updated [[Cn, Operator, Nature, Departure airport, Destination airport, Source, Narrative]]

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